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From: | Eduardo lavratti |
Subject: | Re: [Paparazzi-devel] motor command error on hexa------work arround progress |
Date: | Mon, 25 Mar 2013 09:33:17 -0300 |
I updated the my local copy yesterday. ( i am using master)
Thank for you considerations. > To: address@hidden > Date: Mon, 25 Mar 2013 09:14:34 +0100 > From: address@hidden > Subject: Re: [Paparazzi-devel] motor command error on hexa------work arround progress > > Hi Eduardo! > If the problem is still actuall, try to checkout the latest > actuators_mkk.c file from the master branch. > I've added the i2c submission control, so the actual queue length could be > leaved unchanged. > I've also experienced problems with 8 mkk controllers, they a very > sensitive to the bus speed. With the 400kHz there going to be the bus > errors anyway. I've had problems with 8 mkk sometimes even with the bus > speed about 60kHz. So try to let your bus speed down. But when you let > your bus speed down, and it is not sufficient to control all the motors > once per periodic time, the queue length increase is not going to help. So > then you have to use the fixed actuators_mkk.c file. > But anyway, I've experienced a crash with the stock MK autopilot because > of i2c errors problem, so imho the solution with more than 6 mkk > controllers is not reliable enough. I wouldn't recommend that. > Regards, > Sergey > > _______________________________________________ > Paparazzi-devel mailing list > address@hidden > https://lists.nongnu.org/mailman/listinfo/paparazzi-devel |
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